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A Little Joe II failure investigation presentation was made at MSC July 13 in which General Dynamics/ Convair (GD/C) and MSC's Engineering and Development (E&D) Directorate presented results of independent failure investigations of the mishap which occurred during Apollo Mission A-003 (Boilerplate 22) on June 22, 1965, at WSMR.
The GD/C investigation results were presented by J. B. Hurt, Little Joe II Program Manager, in the form of flight movies and a slide talk. The data made the following points: - At approximately one second after liftoff, the Fin IV elevon moved in a direction to cause the observed clockwise rotation and at 2.5 seconds reached the fully deflected position where it remained until vehicle breakup. The E&D investigation results were presented by O. P. Littleton of the Guidance and Control Division. In summary, results of the E&D investigation were stated to have confirmed the findings of GD/C although different computer methods were used. Littleton agreed with the conclusions of GD/C, but emphasized that an electrical malfunction within the Fin IV hydro-electrical servo-loop could not be discounted as a possible source of failure at that time.
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